
Our new homepage is online!
After a long period of planning, lots of ideas and countless hours, the time has finally come: our new homepage is live! We are looking forward to your feedback!
A natural gas CHP unit with 2 MWel and 2 MW waste heat as well as an absorption chiller (AKM) with 750 kW cooling capacity are installed in the new energy center in the middle of the industrial plant. The CHP covers the electrical base load (approx. 50 %). The site produces 380 million light bulbs in 3 shifts throughout the year. The waste heat is fed into the existing heating network and covers approx. 90 % of the heating requirements. The CHP also supplies an absorption chiller. A new 13/19 °C cooling network will be installed throughout the entire facility. The centrally generated cooling is intended to cover the base load of the 32 compression chillers distributed throughout the plant.
After a long period of planning, lots of ideas and countless hours, the time has finally come: our new homepage is live! We are looking forward to your feedback!
Rising energy and raw material prices can be counteracted by using sustainable energy technologies and thus reducing CO2 emissions. This not only significantly reduces cost explosions, but also reduces your own ecological footprint. Pioneers in the dairy industry are also focusing on this.
Some people are simply indispensable in a company - Thomas "Tom" Winkler is one of them. He started with us around 25 years ago as a young engineer and grew from project manager to project manager to authorized signatory. With a great deal of passion and dedication, he has become a permanent fixture in our management team. But above all, Tom is a real team player who always has an open ear, is always willing to help and makes everyday life easier with his good humor.